Hamble SailZone [GK24 logo]


Forethought 2009 log


This is now the story of year 13 of owning a GK24

Index

Race 1 and 2 Frostbite
Race 3 and 4 Frostbite
Rope off prop and fitting speed transducer
Race 5 and 6 Frostbite
 

Since I was made redundant by NXP and given a nice payoff for leaving, and managed to get a new job at Quest Geo Services of Liphook (www.qgsl.com), I decided to spend some of the money on the boat. On order are new sails and new electronics.

Saturday 10th January - sea trials and refuelling

I took the boat up and down the Hamble using the new Simrad TP22 autopilot but it does not yet seem to be listening to the output of the GPS for navigation to waypoints. Probably a miswiring or NMEA overload somewhere( actually RTFM , press the auto option and then nav option button), lots of  identical 4 core cables running around the place carrying NMEA to and from GPS, speed log instrument,  tiller pilot and AIS/GMDSS VHF. Coupled to this lot will be a Simrad wind instrument which will also control the autopilot in one operational mode.

Royal Southampton Frostbite Series 2009

Race 1 and 2 , Sunday 11th January 

Owing to a crowded Ocean Village we were forced to start from Hamble, where the crew discovered the mess that Eastleigh Council have made of the parking in Hamble which is not liked by anybody and was not asked for by the Parish Council. It makes Hamble even more unwelcoming to people wanting to visit to come sailing  or just visit the village. One crew member took half an hour to locate a space that was not a pay space so did not have a 4 hour limit on it.
Spaces on the Hamble Common have been 'replaced' by painting car parking bays and putting up 'P' signs  on Spitfire Way where you could park anyway.....

We still arrived at the start  line after 40 minutes from the Hamble quay.  

This year we started with the same crew as for the Round the Island, and we raced with the number 2 genoa and and a non-reefed main. Some of the other boats were using a single reef.. The racing started in 15knots  gusting  20 and increased to 20 knots gusting to the high 20's. In the first race we flew the spinnaker, and apart from one from the hatch launch that took a long time to tidy up before we were able to gybe onto the correct tack for the leg, everything went pretty smoothly . By the end of the second race the genoa by itself was rather too large.  But we still flew the spinnaker downwind and were rewarded with 7 knots on several occasions.  At least by the time we arrived at mark 3, the RIB had managed to put it back in place after mistakenly removing the mark as class 1 was arriving. It had been used as the first mark in race 1 and the RIB crew didnt realise it was the last mark of race 2.

After the race we headed back to Hamble and switched the VHF into AIS scan mode. Immediately the chart plotter started squeaking as the Red Jet came up from behind on a collision course. It also squeaked as we passed stationary oil tankers as some of them were still transmitting AIS "under way" flags although they were obviously tied up at the time. Bad boys.

Final approach to the mooring was messed up by the windage causing the boat to come to a stop broadside on to the wind. It took a fair effort to put the mooring lines over the cleats.

Race 3 and 4, Sunday 25th January

The night before a set of fronts went through and the wind had dropped from 28 knots on Bramblemet back down to something we could go sailing in.

We managed to all get to the quay, the traffic wardens were out at 0830 on a wet windy sunday morning. What used to be a quick park up and get sailing is now a 20 minute walk from the nearest free parking space.

Les was not around having suffered an ear infection he claims from the first race, but I did feel then that he was not hearing as well as usual on the 11th. Anyway we set off in the usual fashion and arrived at the start line without incident.

Race 3:

As usual we decided to go for a clear-air start at the pin end of the line and this time there was several forces different in the wind strength  between each end of the start line. The wind was very shifty and there were big holes all around the course. We crept across the line while all the other boats shot away in a gust. The course was a zigzag across Southampton Water. A few ships passed up and down while we were racing and this was to be our final straw later on in the race.

Snapped Shackle

bent shackle
 pin On one tack as we were coming onto the layline for a windward mark, the bronze snap shackle holding the bottom of the mainsheet on the traveller (quick release for cockpit living in harbour and use as a crane hook)  got twisted around the traveller and was opened and then the operating pin was snapped off. Fortunately, I had left a couple of shackles close to hand inside the cabin.
 But we still lost ground and had to do a tack to get back to the mark. We sailed some distance with Duncan holding the mainsheet and Steve fitting the shackle.
We had the No1  genoa up because of the light conditions around the start - it caused some grief with stiff hanks, and we were overpressed most of the rest of the race.
On the final beat, we had the RFA Eddystone ship coming in from the Solent, a container ship of about 60000 tons coming down from the docks and a Red Funnel ferry coming in fast from the Solent. We lost about 5 minutes as we could not sail a proper course to the mark, going behind the container ship and the Red Funnel and in front of the RFA. On the run back to the finish,   Steve put the spinnaker on upside down (last done in 2000 in a Frostbite Series race ... ) and we decided things were too far gone so  we decided to retire being thoroughly last and needing to sort things out a bit before the next start .

Race 4

We changed down to the number 2 around the start time and this time once the Class 1 had got going with a big windshift messing up their start causing a late postponement, we got away and things went well until near the end when we sailed into a hole, and spent a lot of time crawling at 3.5 knots instead of 5 to windward and 7 off the wind. Again it took a long time to get to the finish. We had then got three soaking sails although the No1 was only damp, the spinnaker was dripping and the No2 was running wet. I put on the heater and pumped about 2 gallons of rainwater out of the bilge, dumping it in the sink which then blocked. I managed to clear it by applying suction from one of the syphon pumps which I use to clear the bilge. I thought that would be the worst thing . We dropped Duncan and Nigel off on the quay , and went to the mooring, But when we got to the mooring things went wrong. The first mooring line went on the stern cleat OK, after we had approached the mooring going astern. The second somewhat longer backup line demanded by the insurers  managed to wrap itself around the rudder and then despite remembering to put the engine in neutral, it seems to have been knocked into astern. It succeeded in wrapping the spare line round the prop. I asked for the engine to be turned over in gear with the stop lever pulled out to unwind the twisted rope but it started because the stop lever was not pulled out. A short time later it stopped again. A second set of attempts working with the engine in gear but not starting unwound the rope revealing a cut-off end .  The rope cutter must have worked. The other end of the rope is still  firmly attached  to something on the sterngear - the prop shaft rotates but the rope stays  fixed.


Stockhausen and Burns Night 31 Jan - 01 Feb

It was a cold Saturday afternoon. I took Catrina out with me to help move the boat. .We fitted the outboard to the bracket on the stern of Forethought, but in retrospect,it could have been more effective  leaving the outboard on the tender and using it to push Forethought from alongside. The tilt angle of the engine was left correct for use on a dinghy. The result was we made a small rooster tail , the outboard throwing water and air. We crept against the wind, it was slack water so that was not a problem.
Catrina helmed, and I operated the engine , keeping my weight above the outboard to improve its grip.

We arrived at the Royal Southern piles, just as Shirley and Ashling walked down to the clubhouse, so after tying up Forethought, with about 0.5 metres of water under the keel, we paddled the dinghy ashore - did not notice there was only one rowlock before we borrowed the dinghy. Sat in the bar with a Coke and watched the Fireflies racing out on the river .

As twilight approached , I collected a load of gear and took it out to Forethought .  I threaded the cable through for the paddlewheel transducer up to my new  instrument panel. The new sounder indicated 4.4 feet and then the keel grounded about 1630 . I waited for the tide to fall clear of the hull - fortunately there is a pontoon tied alongside the piles , so I could step off  and look without getting mud anywhere.

I then drilled a pilot hole for the paddlewheel transducer from the inside of the hull checking for vertical and horizontal clearance under the shelf where the heads is fitted . I had to take the handle off the hand drill to get it in. After a lot of slow drilling , it broke through. I dropped a split pin through the hole because I knew it would be easier to find in the darkness from the outside.

I prepared a crate of tools and essentials for the job, taking exactly what I wanted as Hamble mud decontamination is time consuming - required if you forget anything before going back on the boat to get it.

 Two hours later after putting on some old and disgusting oilies, I scrubbed the hull with a pad using my disposable gloves that I bought from an agricultural supplier which go all the way to the shoulder. (would have made James Herriott's life easier..)
I worked along the hull  as the water receded leaving the usual 2 inches of Hamble mud on the slip.

When I got to the prop I put the gloves to one side, pulled out the trusty N95 from in my jacket and snapped a picture.  The rope was wrapped around the shaft between the rope cutter and the P bracket. It had been cut by the cutter but had then jammed in the gap. As it needs a gap to allow for the engine mounts to take up when motoring, this basic rope cutter had reached its limit. After a lot of hauling the rope came clear , wiggling the prop and heaving.

rope wrap 

Then I changed to fitting the paddlewheel transducer. Locating the splitpin I had previously placed, I loaded up the 18 volt Black and Decker with a 50mm hole saw and blipped the trigger a couple of times. The drill has a positive lock when the trigger is released , snapping to a stop. In keeping with the rules of  Murphy, the grip of the drill was not exactly on the centre of the flats of the hexagonal drive shaft so when I pointed the drill down after blipping the trigger, the hole saw fell in the mud. A quick rinse in the river and a wipe with a rag and I was back in business. I started the saw and was immediately showered in fibreglass dust. Ugh. I carried on but upwind and after a few tens of seconds, the saw cut through. I then scraped the antifoul around the hole back to the epoxy and loaded up the through hull fitting with Sikaflex which begins life as very sticky so the fitting stayed put . I went off to decontaminate my boots and salopettes, especially inside the trousers where the mud seeps. Stomped around on the pontoon to shed more mud, and went back on Forethought to put the nut on the through hull fitting.  having done that I then had to go out , wipe off excess Sikaflex and then dab on a quick bit of antifouling.
Another decontamination and then that was it.

Job done it was then waiting for the tide to come in.  So I had a thermos load of  chili con carne and rice defrosted and heated earlier at home. Then to read for a while and play with the features of the new GPS.

At 2100 I decided to turn off the heater and lie comatose in a sleeping bag until 2300. So I did that and I dozed and slept for the next 2 hours. I woke up and noticed the happy noises coming from the club house. I realised that it must be the Burns Night celebrations.

 I looked outside and the tide still looked like it had a long way to go.  So I had a cup of coffee and  turned on the 1970's FM stereo. I tuned around and there was someone talking about Stockhausen on Radio 3 . They played a recent recording, and the clicks of the heater and the echosounder transducer , the squelch crunching on the AIS channels on the VHF added to the performance in a strange way .  A mystery vessel came up the Hamble and docked on one of the outer pontoons at Stone Quay according to the AIS display.

At 0100 or thereabouts Forethought slipped back its keel and I dressed up in the clean waterproofs and thermals I had bought with me. I took the boat off the piles. This time I remembered to undo the main halyard from the piles and tie the dinghy back on Forethought instead of the pontoon.

I went out and motored around the river for a bit checking for vibrations - none found so went up to the mooring and tied up at 0200.

While I thought that I did not feel tired , when I found  the heads was not pumping water in at 0220 it made me feel very tired. It necessitated a partial disassembly of the pump, and then a clean up of the flap valves,  before finally going back in the sleeping bag for some sleep.

I wanted to get up again at low water, about 0730 to fit a replacement for the mooring rope previously mentioned - it is easy to reach the top of the chain part of the riser at low water to shackle new lines to the chain. The ebb tide against the wind woke me with the happy chuckle of water slapping the hull by my head at 0500. At 0730, the air temperature in the cabin was 4 degrees C before I put the heater on. I went out, fitted the new mooring  rope(3 metres spliced to a thimble and an eye splice).  All jobs done from that set, I went home.


Race 5 and Race 6 : 8 February 2009

For a change it was cold and calm to begin the day. Only Duncan and Steve came out this time. We motored out to the start which was delayed by an hour to wait for the wind which started off as southwesterly on the west of Southampton Water and southeasterly on the east of Southampton Water.  The topping lift block at the top of the mast has completely given way and so we had to unshackle the end on the boom to get the boom to drop.

On the way out we failed in trying to calibrate the autopilot -either we went too fast or turned too fast in the required 540 degree circle, which mystified other boats around us. A course was eventually set with a beat of 0.6 miles .

Race 5

We set off from the port end of the line just behind Glass Onion and we kept clear wind.  As we neared Hamblecliff buoy, the windward mark, the wind started going fluky but we still got round OK.  Occasionally there would be moderately strong gusts but most of the time we were sailing under hull speed.  We finished with other boats for a change. Perhaps the scrubbing of the hull helped..

Race 6

The second race was pretty uneventful apart from the Red Funnel ferry having nowhere to go while we were going up the beat, and we lost a couple of minutes tacking behind it. By the end of the race the wind had increased to about force 4. We finished and went home . It was a short race.  No other problems.

Race 7 and 8 : 22 February 2009

New Sails !  I had ordered some sails from Quantum  before Christmas and they arrived. On the Saturday before, the whole family went out to Forethought and Ashling and me fitted the battens to the new sails. I had ordered a new mainsail, No.1 and No.3 genoa and a spinnaker. The  No.3  has battens as well.
On the Sunday, only Steve could turn up, and there was no wind.

Again on the way out we tried to calibrate the autopilot, and failed again. I think there may be some other magnetic influence around the autopilot.
Trying to use the autopilot with control from the GPS resulted in going off track until the cross track error would compensate for the compass error and the boat would finally go on course.but 100 metres off track. As we were playing around in Southampton Water this meant we kept on trying to ram the tug Thrax that was moored to a buoy 100 metres to starboard of the direct track to the waypoint I had selected.

There was no wind  but it was mild and sunny, and the race start was delayed. The result was that  when the wind did fill in, we only had time for a pair of  two leg races, to a windward mark and back. There was a good breeze, so we set the new main and the new No.1 but keeping with the old spinnaker because we were short handed and the new spinnaker bag needs some thought as to how we clip it on.

Race 7

We started a bit late and went out into the deep channel. For a while we were keeping up but eventually we sailed into a hole in the wind and slowed right down. In the gusts, we had 5.5 knots on the log, in the hole about 2 knots.

Race 8

We started even later and the story of the race was much the same.

Interesting examination of the hull core

When I fitted the paddlewheel transducer, I kept the core cut out by the hole saw and later on  I filed down the hull surface at a shallow angle to more clearly show the cross section  of the surface layers. This was gelshielded 10 years ago and the laminate seems not to be affected by osmosis still.

From left to right ...
Surface - rough because many coats of eroding antifoul not sanded down.
Dark blue : International Micron
Pale blue : International Micron .
Grey: Antifoul primer
Green : Gelshield
Grey smooth : Epoxy filler
Grey rough : Epoxy filler
Green : Gelshield
White : original hull layup

Hull section
Looking at the same thing side on : the whole antifouling  through to hull layup is about 1mm
Note the pores in the hull layup, some with green Gelshield epoxy in them- possibly the origin of the osmosis in the first case. The red stuff is paint from the hole saw.
Slice through GK24 hull
Images courtesy of the 1cm super-macro mode on my Samsung NV-S7 camera which has a Schneider-Kreuznach lens on it (this company's lenses normally used for movie cameras). This makes up for the slightly noisy image sensor and the habit of the viewfinder blanking out at +5C and at other times when the camera is being heavily used in the middle of Irish peat bogs.

Race 9 and 10

I had decided to order a new number 2 and a boom cover from Quantum to go with the new sails. By accepting they would make the sail sometime over the next 10 weeks I got a discount.
I was slightly concerned we would need the older No.2, although it is still quite good.
But it turned out to be quite windy. So Steve and myself again were struggling against the elements, with the new No3 up and a reef in the main. As it all went up we lost the genoa halyard which took a bit of catching in the breeze. Then we noticed the second reefing line had crossed the first reefing line so that  we could  not have reefed  again. We managed to fix this then we went racing. At first we were quite in control of things, and were keeping up with the trimaran that was racing as they needed to be so careful in the fluky gusts up Southampton Water. As the race went on we noticed the white horses were building as the wind blew across the Water (about one mile fetch) and the sailing got harder.  We ended up doing over 7 knots on a dead run with a reef in the main and the No.3 goosewinged.  At the end of the second race we broached and the boat lay over on the run just on white sails. I think we were getting tired.

Back up the Hamble we stopped at the Royal Southern pontoon and cleared up in the shelter offered by the club buildings. Then off to the mooring and by this stage the wind was pushing the bow off the wind so we couldnt come in slowly heading up wind.
We  ended up blowing down wind bows first onto the mooring with the engine going astern to slow us down . We stopped and then the boathook bent and Steve dropped it in the river. Fortunately it floated and he was able to go back and get it about 10 minutes later as the wind and the tide balanced it quite nicely near the boat.

Hamble River SC Wednesday Evening Series

Race 1:  1st April 2009

I was expecting problems arriving on time on Wednesday evening, but I ended up attending the Ocean Business show in Southampton on Wednesday, so I managed to arrive at Hamble in good time.
The usual crew were back , from illness or work so we set out with a full crew and the new sails for the first time. Despite sailing off to one side of the course in the hope of finding more favourable tide but ending up with less wind, we still managed a second place.


Race 2: 8th April : Not Really Racing

This time I was only able to arrive by about 1750 so we decided to go for an arrangement where the I would give a key to Steve and the crew would get the boat off the mooring. Unfortunately there was a miscommunication on leaving the berth, and it was quite a low tide, so the stern ropes ended up round the propellor again. Fortunately part of the miscommunication resulted in the boat still being moored at the bows. So the evening turned into a long and cold session of clearing rope from the propellor. I did not like the idea of the boat being moored by the propellor so I felt we had to clear enough rope to make sure we could leave the boat moored more or less normally,  but with more or less rope hanging from the propellor.
We started with weight on the foredeck and this brought the propellor into view. One of the stern mooring ropes came off the prop and so we had a bow and stern mooring line. So we shifted to using a spinnaker halyard across to a nearby pile and weight at the bows. A lot of sawing with a junior hacksaw and eventually we had a lot of pieces of rope and two shivering people.

There is still some rope on the propellor shaft but the propellor turns fairly freely, and we have left it as the boat should be coming out of the water for a 10 year insurance survey and tidy up quite soon. Again I am glad I changed the P bracket a while back as the old one probably would have come loose with all this mistreatment.
It looks like some practice in tricks and concepts of leaving moorings is needed .

Sunday 12th April : Repairing the mooring

Steve and I bought  17 metres of rope and a shackle and thimble to repair the mooring. When we got to the boat and looked harder we realised that one of the other riser ropes had been chewed so needed replacing. So back to the Chandlery Formerly Known as Aladdin and another four metres of rope and another shackle and a thimble were purchased. Total cost was about £35. I spliced the ropes and we worked on replacing the risers, waiting until the tide went out enough for us to get at the end of the chain. Once that was done we scrubbed the more easily accesible part of the hull, and went away,

Race 3:  15th April : From wind to zero

I was able to be at the pontoon really early this time , as we had had a couple of days in London so I was not in work. There was quite a strong breeze, enough to set off with the Number 2. Early on while preparing the spinnaker pole on the beat, Les repeated a little skid on the foredeck and ended up hanging from the spinnaker pole with Steve hanging on the uphaul keeping him from crashing.  We made reasonable speed but as the wind decreased, we were losing power, but we just made it around the last windward mark before the breeze died. With the GPS showing 1.3 knots and the water speed at 2.0knots with the spinnaker up we decided it was time to change down to the light 3mm spectra spinnaker sheets, which stopped the spinnaker from collapsing. We sat around for a while as the opposition either crept off on the last of the breeze or drifted outside us in stronger tide standing still over the ground. We were encouraged by the sound of the Class 1 leaders coming through, as they had more wind upwind and inshore of us. We waited and the pressure came back on as the sun set. Hanging onto the sheets using water bottles as handles - needs something like kite string handles to take the strain on the thin sheets, we made it back at 5 knots through the water, 4 knots over the ground.

Sunday 19th April : Photoshopping the deck

Back in 2001, Forethought looked like this :
 
I thought the boat was Photoshopped or equivalent, but then I realised it had new deck paint. As Les had slipped on the deck in the last race, and partly this is down to his boots, but some of the slip was due to the slightly shiny deck.
I spent the afternoon in a cycle of using a Dremel tool to mill out cracks in the deck, then filler and sanding then paint. In the sun and wind the water dried and I was able to do the foredeck panel and the two side panels of the deck before running out of paint and masking tape and getting bored with the whole game.

Wednesday 22nd April : Committee Boat duty

I tried to leave early from work but the race officer was not able to wait 10 minutes for me, heading out of the river with only Steve and another on board. So I went home in disgust. I had tried extra hard to be early but it probably never will be possible for me to make it on time.

Sunday 26th April : Beaulieu Boat Jumble

I managed to buy some antifouling paint and a new topping lift for when Forethought comes out of the water for maintenance including the replacement of the rigging over a weekend soon.
I collected the new boom cover from Quantum over the weekend.


Some Wednesday races followed but the performances became more dismal as the weed grew.

But we discovered that the autopilot now will steer a course to the chartplotter's command with only a few metres cross-track error. A major step forward.


Mid-Season haul-out

On the second May bank holiday, I arranged for Forethought to come out of the water at the Elephant Boatyard, being near to the Aladdins Cave Rigging shop. So I did a lightning attack on all of the things that needed doing out of the water.

Day 1: Thursday :

The tide allowed the family  to drop the boat off at the boatyard.

Day 2 : Friday : 

nothing done

Day 3: Saturday

Antifouling scraping,   removing vinyl names from the sides and transom (done by Catrina)  using a scraper and excessive force. Sand  remainder of blue stripe on side of boat.  Paint one coat of blue paint over the area where  name was.  Paint transom white areas with International Toplac as this resists the dirt from the engine exhaust better than the gelcoat. Extended the Toplac area down the sides of the hull into the region where wave slop allows weed to grow above boot topping -weed doesnt stick to it either.

Took rigging off mast and took it to Aladdins Cave Riggers - 'work to take about a week'.  Broke one of the spreader ends taking it off. Discovered it was irreplaceable. All of the locking nuts failed as I took bits off , so bought new ones.  Aluminium main halyard sheave had also partially collapsed resulting in amazingly difficult main hoists over the last couple of years.

Fitted bracket for new wind instrument to masthead.

Day 4: Sunday

Painted entirety of blue stripe . Two coats of antifouling  on the lower hull. One coat of boot-topping antifoul.  Stuck new vinyl name sticker on hull sides and transom.  Log transducer leaking - I did seal it with Sikaflex from an old tube in the dark when I fitted it and it seeped at first  but the seep slowed down . On removal, the seep stopped because it had silted up.

Day 5: Monday

Came back and checked it was OK and went away again. Made a new topping lift out of  3 mm dyneema with an added wear and handling polyester sheath using rope from one of those English Braids bags of string at the Boat Show.


You can see in the picture the extra shiny Toplac near the transom just above the boot topping stripe.

Day 6: Tuesday

Tried to get mast spares , there is now nothing left for 30 year old Proctor masts. Made up a spreader end using 5mm aluminum sheet.  Actually things like Proctor main halyard sheaves are the same size as modern Selden ones but the people who sell masts seem to be too stupid to read their own catalogues which can be found online.

Day 7: Wednesday

Played around with DIY anodizing using 60 volt power supply , kitchen chemicals and a lot of care against electrocution. (at 25 volts I could feel the tingle with wet hands) . Thickness of anodizing film depends on polarizing voltage like aluminium electrolytics where the film is thick enough to block the working voltage. In this  case the current never dropped as there were too many holes in the oxide layer or I was doing it too fast, and I was in danger of boiling the electrolyte with the 60 watts of power going into it...

Day 8 : Thursday :

Fitted spreader end, took first pass at  main halyard sheave by filing it down to sort of circular. Pulled the wire for the new wind instrument down the mast after false starts caused by the last piece of string that holds the wiring bundle together inside the mast still being there, stopping the 10 mm diameter plug on the end of the cable from going down the mast. Very frustrating with going back and forwards 12 metres to pull on different strings.

Day 9:  Friday:

Non-delivery of rigging as wrong parts sourced from supplier to the riggers.

Day 10: Saturday:

Went to the original Aladdins Cave Foulkes chandlery barge and eventually found a sheave with a smaller hole for the main halyard. Drilled out the hole and then fitted the sheave  and started  replacing the bolts holding the chainplates to the deck as there was some sign of corrosion. Discovered that Force 4 dont do all the sizes of M8 bolts and so I had to put them all back. Some are a bit corroded, but strangely shiny. Ordered relevant bolts from A2A4.

Day 11: Sunday

Went for a walk in the New Forest with ex-NXP colleagues ending in a meal at a pub.

Day 12: Monday

Day 13: Tuesday

Still no rigging

Day 14: Wednesday

The rigging suppliers computer system is down. 'no point in going to Chandlers Ford to ask for the parts as they wont be able to do anything''  I am starting to consider asking for the old rigging back to be re-fitted as I have now missed another Wednesday evening racing owing to problems in the rigging department.

The new stainless bolts have arrived so I can fit them tomorrow, hopefully the rigging will appear and I can fit that back to the mast in the slight hope of getting the boat back on Friday.

Then all that will be left if the mast gets back in ever is wiring through the cables for the new wind transducer and powering up the instrument bus from autopilot through to wind transducer.

Day 15: Thursday

The riggers phone to tell me the rigging is on course for Friday AM. So is the high tide so it all comes together at the Elephant Boatyard's mast stepping and unstepping barge. I fitted the nice new bolts so I wont be worrying about crevice corrosion while broaching in the RTI . Hopefully I will get the boat back on Saturday and then fit the masthead wind instrument and thread a couple of wires for it through the lockers.


Round the Island

Fixing the mainsheet broken during the RTI
We pulled a fitting off the boom and so had to use the spare fitting. The end of the boom was so corroded I decided to cut off the jagged metal , file down the mess and fit a webbing strop instead around the end of the boom.


Mike James June 2nd 2009